
Rowdy S13
Audioholic Chief
This was a busy/eventful weekend to say the least! As you can see we did indeed get the car running, but that is getting ahead of ourselves. One of the first things this week was my car finally being deemed totaled! So that meant getting a new car, which I was going to put off till Monday since I wanted to work on the TA. For some reason I decided to check out one more car on Friday before going by Chris, and then that led to me buying the car I had looked at earlier in the week. That meant that I was MIA for Friday, and want able to get there till Saturday afternoon. So here is the car I picked up, a 2003 Acura CL Type-S with 71,000 miles.
But enough about non TA related things, and on to the good stuff! The work this weekend actually started during the week, when Chris installed the main distribution blocks and wired a few things in. Friday he worked on more wiring, but mainly just crashed (hard to stay motivated on Fridays). Saturday he hit the ground running, determined to get the car running this weekend. Since I wasn't there I didn't get any pics of his handy work, but he finished wiring all of the main power and grounds. While he was wrapping that all up I arrived and started working on the fuel pumps. I had already made the mount for the pumps a few weeks back, but I still needed to mod the upper part of the mount. More or less we removed all of the metal lines that come out of top of the pump mount/tank only leaving one that acts as a vent. Of course that left a bunch of holes that needed to be filled, so I started by welding them all up, and those fumes were no fun. After I had sealed it all up I then drilled for the -8 and -6 bulkhead fittings and installed them. After that was done I wired the pumps together, and then plumbed in the Y block. Here is the finished result!
The AN line is just a piece of -6 we threw in there so that the fuel would not dump over the pumps, probably not needed, but what the hell. That is actually the ONLY pic I have of any work Chris and I did all weekend. As you saw in the video above, the car did start and run just fine. There was really no drama in it, which is good. We started by disconnecting the injectors and cranking it to get the oil moving. Once we knew it was then we tried to fire it up, but had no spark. A quick "temp in" of the main harness grounds and that problem was solved. Round two of trying to start told us the coil packs were not right, so we swapped them front to back on both sides and wallah it lit right up!! We are still a long way away from driving, but we needed to hear it come to life.
Now on to Sunday, when I actually took some pics...because I wasn't working
Chris has been wanting to get the car detailed for a while now, and since we are nearing completion he set it up for Sunday morning. David (blue-sun) showed up about 9:30 in the morning, and busted his *** till just about 3:00, and it looked awesome! On with the pics,
Before
Starting the wash
After the wash, and the clay, and the wash, drying it off
Already looks 100 times better
Back in the garage to start the real work

But enough about non TA related things, and on to the good stuff! The work this weekend actually started during the week, when Chris installed the main distribution blocks and wired a few things in. Friday he worked on more wiring, but mainly just crashed (hard to stay motivated on Fridays). Saturday he hit the ground running, determined to get the car running this weekend. Since I wasn't there I didn't get any pics of his handy work, but he finished wiring all of the main power and grounds. While he was wrapping that all up I arrived and started working on the fuel pumps. I had already made the mount for the pumps a few weeks back, but I still needed to mod the upper part of the mount. More or less we removed all of the metal lines that come out of top of the pump mount/tank only leaving one that acts as a vent. Of course that left a bunch of holes that needed to be filled, so I started by welding them all up, and those fumes were no fun. After I had sealed it all up I then drilled for the -8 and -6 bulkhead fittings and installed them. After that was done I wired the pumps together, and then plumbed in the Y block. Here is the finished result!

The AN line is just a piece of -6 we threw in there so that the fuel would not dump over the pumps, probably not needed, but what the hell. That is actually the ONLY pic I have of any work Chris and I did all weekend. As you saw in the video above, the car did start and run just fine. There was really no drama in it, which is good. We started by disconnecting the injectors and cranking it to get the oil moving. Once we knew it was then we tried to fire it up, but had no spark. A quick "temp in" of the main harness grounds and that problem was solved. Round two of trying to start told us the coil packs were not right, so we swapped them front to back on both sides and wallah it lit right up!! We are still a long way away from driving, but we needed to hear it come to life.
Now on to Sunday, when I actually took some pics...because I wasn't working
Before


Starting the wash


After the wash, and the clay, and the wash, drying it off

Already looks 100 times better

Back in the garage to start the real work
